Schmidt Double Snowblower in 1:32

Wiking models features a beautifully detailed model of a Schmidt two stage snowblower in 1:32, which matches exactly the scale of our JC PistenBully 400. Albert bought two of these models on a suggestion by Klaus Bergdolt, who already successfully motorized such a snowblower. The plan is to built a functioning double snowblower.

Drilling Out
Mounting on the Snow Cat
Videos of the First Test Runs

The german magazine TRUCKmodell 3/2016 issued an article by Klaus Bergdolt and me about the modification of the snowblower with lots of advice. It's in German language.

The article can be downloaded here as PDF, with friendly permission by the magazine.


First the snowblower has to be disassembled. Especially the drum shaft shows significant resistance. The end disks are pressed on to the shaft, and the blower drums are fixed by a ribbing. We carefully drilled out one end of the shaft, and then pressed out the shaft on a drill press so far until a drum could be removed. The remaining parts could then be removed relatively easy.

Drilling out one shaft end

Shaft with ribbing for the drums

Parts of the snowblower

Drilling Out

After we had now all the single parts available we started drilling them out. Luckily all parts which have to be modified are made of plastic, which makes the job relatively easy. The chimney is completely closed and has to be opened of course. Otherwise no snow could be blown out here.

Chimney outlet from above

Blower housing and chimney

Blower fan motor cover

Blower fan backside

We mounted the parts in a vise and carefully drilled them out. The rest was removed by using a Proxxon Micromot tool and micro files. The backside of the blower housing must be smooth, for this 1-2 pin marks have to be sanded, see picture below:

Blower fan housing and blower motor cover with the drilled out chimney

At the blower fan the center pivot was removed with a 45°-countersink (see picture below left) to make room for the motor. For the same reason the mounting pin for the blower fan had to be cut off (see picture below right).

Drilling out the blower fan with a countersink

Cutting the pin at the drum gear box shaft

Finally we drilled out the drums to make room for the motors. This is the most difficult part, and therefore we worked diligently. We carefully clamped the drum in a vise by using rubber parts so that they just could not be rotated by hand anymore. Then we drilled in several steps, first with a 4 mm drill, then 5 mm, at low speed and working slowly. Finally we used a 6,5 mm (or 1/4") to get enough clearance for the motor-gearbox-unit with 6 mm diameter. In most cases the top segment will get loose, which can be quickly fixed with super glue. The loose ends of the conveyor srew were also glued together with super glue, of course the paint was removed beforehand with a knife.

Carefully drilling out the drum

After we hollowed out the chimneys the mounting pin was gone. Of course we wanted them to rotate and therefore the simplest solution to simply glue them in a fixed position was a no go. After some brain storming we cut short pieces from 1 mm steel wire and glued them into the base of the slewing ring (see left photo)


To drive the drums we ordered this motor-gearbox units, and this micro motor for the blower fan. We carefully drilled out the gear box for the drums to the outer diameter of the motor-gearbox unit of 6 mm. Albert made a fitting hub for the blower fan out of plastic on his lathe with a 1 mm center bore for the motor shaft. The hub was glued with super glue into the blower fan, and later the motor shaft into the hub again using super glue.

Drive motor for the blower fan

Blower fan hub

Glueing the blower fan motor
Glued blower fan motor

We milled a fitting opening for the motor into the blower housing. The motor was carefully positioned so that the blower fan can rotate absolutely freely. For glueing we kept it in position with tooth picks (see pictures above)

Micro motor-gearbox units to drive the drums

Soldering the wires to the drum motors was quite some fumbling. We stored the soldered wire ends in opposite cavities of the housing to avoid them getting in contact. The motor-gearbox units were glued with super glue in place.

To drive the drums Albert made shafts from 3 mm brass wire on the lathe, with a 1,5 mm drilling for the motor shaft. The drums have different widths, therefore the lengths of the shafts are left 21,5 mm and right 18,5 mm. To drive the drums we used a M1,6 worm screw which we made ourselves.

Shafts for the drums

M1,6 worm screw as shaft driver

Mounting on the Snow Cat

The snow blade can be removed, it is hold in place with a hard to reach screw. After measuring the mounting pins we made a mounting plate out of black plastic on our Stepcraft CNC milling machine. We connected the two snow blowers with a hollow quadratic brass tube by tapping M2 threads into the mounts. We glued the brass tube to the plate and attached it with M2-bolts to the device carrier. Finally we will made a mounting frame similar to the original.

JC PB400 device carrier

CNC-milled mounting plate for the snow blower

A PDF of the drawing with dimensions for the mounting plate can be downloaded here.

Connecting both snow blowers with a quadratic brass tube

Mounting of the double snow blower onto the device carrier of our JC PB400

We made a frame out of quadratic brass tubes to mount the blower to the device carrier. The wires were glued to the underside. They will be connected to the snow cat with a plug.

Mounting frame for the double snowblower

Battery on the platform

We abandonned our first plan to power the blower by the snow cat battery. It is now powered by a separate LiPo 1S battery which we simply put on the platform with a micro switch (see picture to the left).

This is optically not the perfect solution, but it's sufficient for the test runs for the time being.

The snowblower in it's element. A test run could not be performed at this time.

First Test Runs (Video)

The first test run in snow, a light fine grained powder at -6°C, were rather disappointing. The blower housings block up very quickly, and the speed of the motors gets significantl reduced. The right blower fan motor blocked quickly and is therefore already inactivein the video. The snow blower as such is functioning as can be seen by the blown out snow. With the JC radio it is rather difficult to move the snow cat slowly enough. Therefore we simply moved it by hand for test. The next step will be the installation of more powerful blower fan motors.

First Dry Test Run (Video)

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